Post #636
Well!
I was shopping with the wife, the Phone rang... Pieter from DP
Good news? uhmm yes and no, the yes part was it makes more power then it did with the runin mapping, the no part was that my clutch is fked/slipping
(something is wrong with it , reverse is still very awfull, and downshift from 3rd to 2nd is as awfull as reverse)
As the clutch was slipping and the replacement hose also decided to tear again!(old s**t hoses) Pieter decided it was quits for now.
Result of the slipping clutch was 350BHP on 0.7 bar boost, he went till 370, but the clutch was occasionally slipping, so 350BHP is what we have to to do with for this summer, to be honest i was quite dissapointed and as Pieter said the engine was really easy makeing power, he was also a bit dissapointed he had to stop @ 350BHP since there was A LOT MORE IN IT!
I called Marvin and we jumped in the car and drove to Nijmegen again, car was already outside waiting for us, we had to fix the leaking FK#$%&$%&@$ hose again, so crawled right back under and again it was the same s**t hose that had a tear in it, removed it a put a new hose on it, and we fixed that, bled the system again and we found out that the radiatorcap is not doing its work, and its leaking at the radiatorcap.
We switched the wheels , as i didnt want to ruin the fresh R888 without having the car alligned, as its a 2.5 hour drive from DP to my home.
Thanked Pieter for the great help and service and got a nice hefty bill in return
wich was a lot more then i thought, but his hours arent cheap when working on cars and hes worth it.
Did a testlap around the industrialpark, and the 3rd ->2nd downshift is really horrible.... we still dont know what the problem can be, but it could be very well a FKED clutch, 600 euros down the drain! thankyou mister SACHS
.
As i was still scared about the gearbox/clutch mishap, i took it really easy and still was kinda dissapointed on the power outcome.
But that was before i gave it some beans on the way home, didnt think that the screamerpipe was that loud , until i decided to hit it in 3rd! OOOOH MY GOD! this thing is the god of thunder! and it really flies!
Had a nice drive home, the speedo /rev isnt working, i think the cable got loose on the backside of the cluster, will have to look into that after the weekend, + need to arrange a new radiatorcap.
Last hour of the trip it started raining, which meant wheelspin @ 120kmpu + so i had to take it easy.
Ill try to get some videos up tomorrow of some flybys for you guys, since the bill of DP was a lot higher then expected, i wont solve the clutch problem anytime soon, we will have to drop the gearbox after summer and see what the problem is.
Im having the car cleaned/polished this weekend while Marvin and i are @ the Nurburgring, i then have another 2 weeks holiday and ill will sort some small things out and spend some time with the wife instead of with the black mistress.
I had a few doubts before if i should go the screamerpipe route, but im so glad i did, its really insane!
I only floored it once from 3rd up to 4th, and i can tell you this... its fking quick! and a hell of a lot louder
After winter im back with a new clutch and then will take this thing to 1,2+ bar instead of this pussy boost of 0.7, for now the 350 is more then enough and i will try 2 -> 3>4 gear pulls tomorrow when its dry.
And yes ill make vids!